Performance of supersonic model combustors with staged injections of supercritical aviation kerosene

来源 :Acta Mechanica Sinica | 被引量 : 0次 | 上传用户:baliver110
下载到本地 , 更方便阅读
声明 : 本文档内容版权归属内容提供方 , 如果您对本文有版权争议 , 可与客服联系进行内容授权或下架
论文部分内容阅读
Supersonic model combustors using two-stage injections of supercritical kerosene were experimentally investigated in both Mach 2.5 and 3.0 model combustors with stagnation temperatures of approximately 1,750 K.Supercritical kerosene of approximately 760 K was prepared and injected in the overall equivalence ratio range of 0.5-1.46.Two pairs of integrated injector/flameholder cavity modules in tandem were used to facilitate fuel-air mixing and stable combustion.For single-stage fuel injection at an upstream location,it was found that the boundary layer separation could propagate into the isolator with increasing fuel equivalence ratio due to excessive local heat release,which in turns changed the entry airflow conditions.Moving the fuel injection to a further downstream location could alleviate the problem,while it would result in a decrease in combustion efficiency due to shorter fuel residence time.With two-stage fuel injections the overall combustor performance was shown to be improved and kerosene injections at fuel rich conditions could be reached without the upstream propagation of the boundary layer separation into the isolator.Furthermore,effects of the entry Mach number and pilot hydrogen on combustion performance were also studied. Supersonic model combustors using two-stage injections of supercritical kerosene were experimentally investigated in both Mach 2.5 and 3.0 model combustors with stagnation temperatures of approximately 1,750 K. Supercritical kerosene of approximately 760 K was prepared and injected in the overall equivalence ratio range of 0.5-1.46 . Two pairs of integrated injector / flameholder cavity modules in tandem were used to facilitate fuel-air mixing and stable combustion. For single-stage fuel injection at an upstream location, it was found that the boundary layer separation could propagate into the isolator with increasing fuel equivalence ratio due due to excessive local heat release, which in turns changed the entry airflow conditions. Moving the fuel injection to a further downstream location could alleviate the problem, while it would result in a decrease in combustion efficiency due to shorter fuel residence time. With two-stage fuel injections the overall combustor performance was shown to improper ed and kerosene injections at fuel rich conditions could be reached without the upstream propagation of the boundary layer separation into the isolator. Stillrther, effects of the entry Mach number and pilot hydrogen on combustion performance were also studied.
其他文献
虚假诉讼不是我国民事诉讼实践特有的现象,有诉讼的地方就可能存在虚假诉讼。解决虚假诉讼问题不应强调虚假诉讼问题的地域特殊性,而应当将虚假诉讼的各种情形分类,进行类型
2010年,欧洲等地频发的航空员工罢工潮,使得这些地区乃至全球航空运输的发展遭受重创。据报道,当地时间2月22日起,德国汉莎航空公司约4000名飞行员宣布开始进行为期4天的大罢
<正> 第三次全国苏联哲学讨论会于4月29日至5月4日在湖南举行。会议的中心议题是:“苏联哲学的改革与人的问题”,与会者60多人(包括四位来自西德和美国的学者)。现记会议讨论要点于后: (一) 改革中的苏联哲学的特点与会者一致认为:苏联哲学已经和正在发生的变化的特点是:(1) 对苏联哲学以往历程的深刻反思和对已有哲学观念的重估;(2) 哲学向人学主题和历史性转向和跟进;(3) 哲学变得更加公开、更加开放、更富于参与精神。但与会的外国学者却对这种变化大多持谨慎和保留态度。 (二) 哲学向人学主
在经历了下岗再就业后做了近十年广告人的我,终于开了一家自己的美容美发店。在现今纹绣行业火爆盛行的市场大潮下,随着顾客对纹绣需求的增多,深感自己20年前学习的技艺匮乏,
底层文学作家以民间化的立场来审视和批判现实社会,他们对底层经验的表述,充分切入到对象内部经验世界和情感世界之中,用切近底层的话语表述还原了底层生命个体欲望的真实。
日前在吉隆坡举行的“亚洲天然气研讨会”上,RWE公司业务主管富勒表示,去年全球船厂共交付58艘油轮,创下一项纪录,依照目前新船交付排期和在建的数据,至2010年全球LNG船将增
为探讨刑事速裁程序试点适用的可行性及有效性,本文对广州市越秀区人民法院2014年10月至2015年10月共一年试点刑事速裁程序已结案件与试点前一年同类型案件进行了对比分析,通
以审判为中心的诉讼制度改革,为职务犯罪侦查工作带来影响和挑战,职务犯罪侦查部门应积极应对挑战,从构建新型侦辩、侦诉、侦审关系着手,进一步转变侦查理念、改革侦查模式、
2010年10月1日18点59分57秒,随着指挥员一声指令,搭载着我国探月工程二期先导星“嫦娥二号”卫星的长征三号丙运载火箭,喷薄而起,直上云霄;19时25分许,星箭成功分离,“嫦娥二
从一般性质、逻辑结构、价值评估三个方面对超前认识作了分析,指出超前认识是人的主观能动性的重要表现之一,其目的则是为了把握世界的未来。 From the aspects of general