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美国Flexbar公司对其西得萨斯州150口有杆泵井,进行了最佳操作程序试验,以期改进油井的生产性能。在两年的试验期内,油管漏失减少了61%,杆断故障减少了35%,泵修次数下降了6%。 Flexbar公司采取了以下5条改进措施。 (1) 对生产油井进行诊断分析,对停产井进行预测分析
Flexbar Inc. of the United States carried out the best operating procedure test on its 150-pipe sucker rod well in West Texas with a view to improving the production performance of the well. During the two-year trial period, there was a 61% reduction in tubing leaks, a 35% reduction in bar breakdowns and a 6% drop in pump-repairs. Flexbar has taken the following five improvements. (1) Diagnosing and analyzing the production wells and predicting and analyzing the shutdown wells