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油田注汽锅炉(也称湿蒸汽发生器)是一种高温高压设备,其产生的蒸汽温度高、压力高,对设备的工艺安全性要求高,是一种安全风险较大,需重点研究的稠油开采方式,如何提高锅炉运行的安全性、可靠性,降低运行风险,是摆在锅炉操作者面前的一个十分重要而紧迫的问题。技术人员针对自动化控制系统易产生报警失灵现象、火焰偏烧、锅炉超压运行等存在的问题,制定了针对性措施,取得了良好的效果,共取得节油效益47.7万元。同时,通过措施的实施,彻底杜绝了因火焰偏烧、管线结垢等造成的爆炉管隐患,降低了操作工人的劳动强度,减轻了工作压力,受到了操作工人的欢迎。
Oilfield steam injection boiler (also called wet steam generator) is a kind of high temperature and high pressure equipment, which produces steam with high temperature and high pressure, which has high requirements on the process safety of the equipment. It is a safety risk that needs to be researched intensively How to improve the safety and reliability of boiler operation and reduce the risk of operation is a very important and urgent issue for boiler operators. Technical staff for automation and control systems prone to alarm failure, flame partial combustion, boiler overpressure operation and other existing problems, developed targeted measures and achieved good results, achieved a total of 477,000 yuan fuel efficiency. At the same time, through the implementation of the measures, the hidden dangers of blast furnace tubes caused by partial burning of flames, pipeline scaling and the like are completely eliminated, the labor intensity of operating workers is reduced, the working pressure is relieved, and operators are welcome.