论文部分内容阅读
本文主要从A油田油井的历年上检率和综合返工率写起,通过统计近三年检泵井情况,分析影响“两率”的主要原因,从抽油杆受力情况、井身结构、抽油机工作参数、油井含水、管杆老化程度、结垢、结蜡等方面进行具体分析,阐述了在控制“两率”工作中采取的措施、好的做法、取得的效果,提出了油田目前在控制“两率”工作中的难点、存在的问题、下步对策和工作重点。
This article mainly from the A oilfield inspection rate and the annual rate of the comprehensive write-up, through statistical statistics of the past three years the situation of the pump, the impact of “two rate ” of the main reasons from the sucker rod force situation, well structure , Working parameters of pumping unit, oil well water, the degree of aging of the pipe, scaling, waxing and other aspects of the specific analysis, described in the control of the “two rate” work to take measures, good practices, the results achieved, Put forward the current oilfield difficulties in the control of “double rate” work, problems, the next step countermeasures and priorities.