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1980年大港油田第一采油指挥部对所管注水开发油田上的抽油井,采取一系列挖潜措施,收到了提高抽油井泵效、延长检泵周期和增产原油的效果。 截至1980年底,港西、港中、港东、唐家河、周清庄五个注水开发油田,抽油井占生产井总数的80.49%,每大产油3543吨。与1979年底相比,平均泵效由80.2%提高到87.2%(包括连抽带喷井),平均检泵周期由334.18天提高到375.71天(不包括措施修井12次),经挖潜的183口并,每天增产原油381.83吨。
In 1980, the first oil production headquarters of Dagang Oilfield took a series of tapping measures on oil extraction wells under controlled water injection development fields and received the effect of increasing pumping efficiency, extending pump inspection intervals and increasing crude oil production. By the end of 1980, five water injection development fields in Hong Kong West, Hong Kong, Hong Kong East, Tang River and Zhouqingzhuang accounted for 80.49% of the total production wells and 3543 tons of major oil production. Compared with the end of 1979, the average pump efficiency increased from 80.2% to 87.2% (including continuous pumping) and the average pump cycle increased from 334.18 days to 375.71 days (excluding workover workover 12). After digging down 183 And, daily production of 381.83 tons of crude oil.