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苏德尔特油田由于弹性开采,油井供液能力严重不足,机采参数调到最低仍无法正常生产。采用间抽制度又消耗大量的人力物力,降低了油田开发的综合效益。抽油机减速节能装置将原冲次降低一半,实现连抽,降低劳动强度。贝28作业区目前共安装减速节能装置53口井,泵效提高了9%,检泵周期延长了近300天,节电率达到14%,系统效率提升了3%,实现节能降耗。
Sudeerte oilfield due to elastic mining, oil well serious lack of capacity, machine parameters to the lowest tune still unable to normal production. The use of pumping system consumes a lot of manpower and resources, reducing the overall efficiency of oilfield development. Pumping unit energy-saving devices to reduce the original impact of a half, to achieve pumping, reduce labor intensity. At present, a total of 53 wells with deceleration energy-saving devices have been installed in Pui 28 operation area. The pump efficiency has been increased by 9%. The inspection pump cycle has been extended by nearly 300 days. The saving rate has reached 14% and the system efficiency has been raised by 3%.